左青,左晖.DTDC结构问题讨论[J].中国油脂,2018,43(12):.[ZUO Qing, ZUO Hui.Discussion of present problems for DTDC structure[J].China Oils and Fats,2018,43(12):.]
DTDC结构问题讨论
Discussion of present problems for DTDC structure
  
DOI:
中文关键词:  DTDC  豆粕  预脱层  脱溶层  美拉德反应
英文关键词:DTDC  soybean meal  pre-desolventization layer  desolventization layer  Maillard reaction
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左青,左晖  
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中文摘要:
      对DTDC结构问题进行了讨论。在预脱盘保证豆粕水分不冷凝、豆粕为散状、脱除部分溶剂条件下,按脱溶负荷要求设计预脱盘数量。脱溶层料层高度500~750 mm,搅拌速度10~12 r/min和搅拌叶的形状让物料呈悬浮状,蒸汽密度为650~750 kg/(h·m2),溶剂和水的共沸物的沸点达到67?℃以下容易挥发和汽提,缩短脱溶时间。直接汽层温度达到105?℃,促进豆粕发生美拉德反应。3 600 t/d的DT电机功率从原250 kW降到220 kW,豆粕残溶低于300 mg/kg,蛋白质溶解度达到75%以上,蒸汽消耗控制在203~220 kg/t。
英文摘要:
      The problems for DTDC structure were discussed. Under the conditions of uncondensed moisture of the soybean meal on the pre-desolventization discs, scattered soybean meal, and some solvent removed, the number of the pre-desolventization discs were designed relying on the desolventization layer. 500-750 mm of layer height for desolvent layer, 10-12 r/min of stirring speed and the mixing blade shape kept the meal in suspension. The steam density 650-750 kg/(h·m2) was provided for the solvent and water azeotrope to reach the boiling point 67?℃ and easily to volatilize and strip,and the desolventization time could reduce. The temperature in the direct steam layer reached 105?℃ and improved the Maillard reaction. The installed capacity for 3 600 t/d DT reduced from 250 kW to 220 kW, the residual solvent in the soybean meal was less than 300 mg/kg, the protein solubility reached 75% or more, and steam consumption was controlled at 203-220 kg/t.
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